1 Centre for Gas, Refining and Petrochemicals Engineering, University of Port Harcourt, Nigeria.
2 Department of Chemical Engineering, University of Port Harcourt, Nigeria.
Received on 01 October 2023; revised on 16 November 2023; accepted on 18 November 2023
In the simulated ABB Randall Process before optimisation, it was found that the process initially achieved a yield of 72%, indicating the potential for further improvement and optimization. Replacing J-T valves with an expander, led to a remarkable drop in the DeMethanizer inlet temperature, from -150°C to -274°C, resulting in more efficient recovery of heavier hydrocarbons. This lower temperature was attained through isentropic expansion, with the expander's work driving a compressor to enhance overall plant efficiency. A comparative analysis between the unmodified ABB Randall process and the optimized version demonstrated the clear advantages of the latter. The optimized process exhibited higher annual revenue, increased annual savings, a shorter payback period, reduced energy costs, and a substantial improvement in natural gas liquids (NGL) recovery, with a recovery rate of 96.4%. While the initial capital cost investment for the optimized process was slightly higher, the accrued financial and operational benefits make it a more attractive and cost-effective choice in the long run.
ABB Randall Process; Optimization; Simulated Model; Natural Gas Liquids (NGL) Efficiency
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Harry Uchenna Eze, Ipeghan Jonathan Otaraku and Peter Odiboroghene Muwarure. Optimization of the ABB Randall process of NGL recovery. World Journal of Advanced Engineering Technology and Sciences, 2023, 10(02), 051–057. Article DOI: https://doi.org/10.30574/wjaets.2023.10.2.0287